I was aware of this rust a while ago and had done a few little bodgie repairs to keep it under control but it was time to do the job properly. [Thanks Gary for reminding me that I need to get it done!]
First of all, the window needs to be removed.
From inside the bus remove the pinch weld around the window frame. These windows are only held in by a silicone bead so use a blade to slice between the body work and the window frame. Because of the rust I discovered the bottom edge of the frame wasn't really sticking to anything. I also found some small perspex strips on the sides which must act as spacers. I didn't need to cut these off to remove the window. [Just left them there ready to do their job when I put the window back in]
It's probably a good idea to have someone on the outside to stop the window just falling out once the silicone beading has been cut. The frame will just push out but be careful as the frame is flexible and the windows themselves can fall out of the frame at the top (they appear to be held on the bottom track because I couldn't just lift them out of the frame - no need to anyway.)
Once the window is out put it in a safe place. I needed to clean off all the old silicon which I did with a sharpened piece of perspex - my frames are black aluminium and the plastic blade prevents scratching)
Time to assess the damage - not pretty!
For about a third of the window the top of the sill was basically gone and the rest could not be saved. No option but to scrape clean and then commence surgery!
I decided to remove all the rusted steel from the outer panel (rather than patch it). All the inner panel was cleaned back with grinder and treated with a product call penetrol to prevent further rust. It actually wasn't too bad. I didn't cut all the top of the panel in one go - I did it in sections to leave a guide for positioning the new window edge.
I'll throw a diagram here to illustrate how I tackled the repair.
First piece of steel goes in - it was steel I already had and it already had a fold - a fraction heavier than what was there. I also treated the underside of it with penetrol. I didn't worry about another vertical fold - there was already plenty of steel on the inside vertical. Worked out well because it created a little valley where the welds would be placed.
I only have a stick welder so I just tacked along the new seam at about 25mm intervals. I had read somewhere that if you try to fully weld such joints you'll just end up with a buckled mess [Would have been impossible for me with a stick welder anyway!] I was very happy with the result and I decided that the only thing to do was keep going with the same method. The rest of the sill edge was actually in good condition but I decided that attempting to do the joint on the top of the sill was not going to work. So with angle grinder in hand I kept going. You can see the pencil line I marked for cutting. I ended up putting three sill plates in via this method [Why? the steel I had was only long enough to do it that way and I liked the way it allowed me to keep the existing line as I went.] Next photo shows it all in place.
Next step was to check the window fitted back in before I went any further. Good news!
Hit all the welds with a grinder to make them flush with the existing panel and then use car filler to hide them. Filler only takes about twenty minutes to dry and then sand back with 60-80 grit paper. Actually in my research I was given a worthwhile tip - only ever dry sand the filler - it is porous and will let moisture through it.
Time to mask up and apply primer surfacer. I applied 4-5 coats. The last black mist coat acts as a sanding guide. Sand back with 600-800 grit paper - not a bad idea to use a sanding block to keep the surface even. Any black remaining will alert you of areas require further filling.
Application of the top coat - I only had a touch-up spray can of the matching colour and I was a bit anxious not having it in the proper spray gun but it went on surprisingly well. I had enough for about 4 coats. You have to leave it for 24 hours before doing anything else but I reckon its a good idea to get rid of the masking tape asap. By the way I was using single pack acrylic lacquer.
Disaster struck [well not absolute catastrophe]. I must have put the last coat on too late in the day, then overnight we had rain and all the next day. I ended up with little blisters in the top coat where it had got wet. It was under a tarp but the moisture still found a way!
Left it in the sun the following day and sanded that coat back - not too bad - will have to repeat a filler and top coat to tidy it up.
That's where I'm up to at time of writing. I need to wait awhile before I mask up again and repaint the window recess black [as done in the rest of the vehicle.] Then it is just a matter of siliconing the window back in. Always make sure you use a neutral cure silicon so it is not corrosive on the metal.
The whole process has got me keen to do the complete respray [in 2 pack] - but that's something I'll leave for another time.
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Window frame removed exposing serious rust on sill |
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Overhead view of the rusty sill |
For about a third of the window the top of the sill was basically gone and the rest could not be saved. No option but to scrape clean and then commence surgery!
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Surgery commences: cut away remaining top sill with angle grinder |
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Rusty bits removed from outer panel - remaining steel cleaned up |
I'll throw a diagram here to illustrate how I tackled the repair.
First piece of steel goes in - it was steel I already had and it already had a fold - a fraction heavier than what was there. I also treated the underside of it with penetrol. I didn't worry about another vertical fold - there was already plenty of steel on the inside vertical. Worked out well because it created a little valley where the welds would be placed.
Next step was to check the window fitted back in before I went any further. Good news!
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Beautiful - fits like a glove! |
Hit all the welds with a grinder to make them flush with the existing panel and then use car filler to hide them. Filler only takes about twenty minutes to dry and then sand back with 60-80 grit paper. Actually in my research I was given a worthwhile tip - only ever dry sand the filler - it is porous and will let moisture through it.
Time to mask up and apply primer surfacer. I applied 4-5 coats. The last black mist coat acts as a sanding guide. Sand back with 600-800 grit paper - not a bad idea to use a sanding block to keep the surface even. Any black remaining will alert you of areas require further filling.
Application of the top coat - I only had a touch-up spray can of the matching colour and I was a bit anxious not having it in the proper spray gun but it went on surprisingly well. I had enough for about 4 coats. You have to leave it for 24 hours before doing anything else but I reckon its a good idea to get rid of the masking tape asap. By the way I was using single pack acrylic lacquer.
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Finish colour is on - you got to be happy with that! |
Disaster struck [well not absolute catastrophe]. I must have put the last coat on too late in the day, then overnight we had rain and all the next day. I ended up with little blisters in the top coat where it had got wet. It was under a tarp but the moisture still found a way!
Left it in the sun the following day and sanded that coat back - not too bad - will have to repeat a filler and top coat to tidy it up.
That's where I'm up to at time of writing. I need to wait awhile before I mask up again and repaint the window recess black [as done in the rest of the vehicle.] Then it is just a matter of siliconing the window back in. Always make sure you use a neutral cure silicon so it is not corrosive on the metal.
The whole process has got me keen to do the complete respray [in 2 pack] - but that's something I'll leave for another time.